Citric Acid, the new Evapo-Rust

I’ve been cleaning old tools ever since I was a kid. I fell in love with the way they looked and wanted to make them look better by cleaning all the rust off of them. After all, when they were in use in someone’s shop, the blade was sharp, the parts moved freely and the tool didn’t have a speck of rust on them. It was only after they were left for dead did rust start appearing on the metal making them appear unusable. I knew early on that with a little love, these tools could come back to life.

In the beginning, cleaning the rust off the plane was attacking it with 220 grit sandpaper. With lots of elbow grease I got the job done. Then after a few years, I moved onto using a flap wheel on my drill press. Rust removal was faster but left a cloud of rusted dust in the air. Something I had a hunch was not too healthy to breathe. I tried electrolysis for a while but thought it was too cumbersome and time-consuming hooking each part to a positively charged metal rod and battery charger.

Then while reading internet woodworking forums, I ran across a member talking about Evapo-Rust. I was intrigued and had to give it a try. I bought a gallon of it, poured it into a container, dropped the parts in, and let them set overnight. The results were amazing! Nothing I had ever tried worked so well with so little effort. There was only one problem; the price. I bought a five gallon bucket form a company called Nebraska Hotrod for $65.00. It would last about five servings worth of tool cleaning, pouring about a gallons worth of it in a container at a time.

Then this spring I read about citric acid. I’ve heard it mentioned before but I was so in love with Evapo-Rust that I thought nothing would work better. But the economy was tight, my wallet was thin and I was open to the idea of using it. Plus I was curious to see how it would compare to my beloved Evapo-Rust. I looked in my local grocery store for it but came up empty. I was told that it could be found at health food stores but eBay was easier and I found it available there. I bought 15 lbs of it for about $42.00 and received it within a week.

I poured one cup of citric acid in about a gallons worth of water and dropped my parts in just like it was Evapo-Rust. I use a 30″ window planter box as my container as it’s long enough for #8 jointers. I waited overnight for the results and was pleasantly surprised! My parts turned out just as well as if they had been sitting in Evapo-Rust.

The true benefit of citric acid is the price.  A cup of citric acid weighs about one pound and a five gallon bucket of Evapo-Rust would last me five servings worth of tool cleaning. So when you do the math, A gallon of Evapo-Rust cost me about $13.00 ($65.00/5 gallons) while a pound of citric acid cost me a meer $2.80 ($42.00/15 lbs). Now that’s a price that I can live with.

Restoring a Stanley No 7 Jointer Plane

Every time I see an article in a woodworking magazine about restoring an old plane, it’s usually a Stanley No 4 smooth plane. While a smooth plane is probably one of the most important planes to own, it certainly shouldn’t be the only plane you have in your arsenal of tools. A jointer plane is extremely handy for jointing the edges of boards straight as well as leveling the tops of wide panels flat. In fact I probably use my jointer just as much as I use a smoother.  So I decided to write a blog and show how easy it is to refurbish an old jointer and put it back to use.

The first thing I do when cleaning a plane is take it completely apart. Remove every single bolt and screw you can and lay them on the bench so you won’t lose them. Don’t worry about not knowing where each screw will go as the guts of a plane are quite simple and easy to put back together.

Next you need to get yourself a product called Evap-O-Rust. I buy it in a five gallon bucket as I clean a lot of tools but a couple of gallons at your local auto parts store should do you just fine. Fill a container with the Evap-O-Rust and submerge the parts in so that they are completely covered in the solution. If you don’t have the part completely covered, you will end up with an oxidized line on the part where the air and the solution meet. It’s also important to make sure that the parts of the plane are not lying on top of one another in the solution. You want to make sure that the Evap-O-Rust has the ability to penetrate the entire part. Let the parts sit in the solution overnight.

Once the parts have soaked overnight, take them out and wash them under the tap to remove any residue from the part. You’ll notice that the parts will be completely clean from rust but will have a dull finish to them. I like to take them over to a flap wheel sander and buff them to a nice satin shine.

After buffing the parts, wipe them with an oil protector called Kramer’s Antique Improver. I have been using this stuff for twenty years and have never come across anything that works better or is simpler to use than Kramers. It simply brings the metal and wood back to life. After wiping all the parts with Kramers, put the majority of the plane back together.

Now that the plane is clean, you’ll need to make it work. The first thing to do is grab something that is perfectly flat and place soaking wet 220, 320, 400, and 600 grit wet and dry sandpaper on top of it. I use an old marble window sill but the top of your table saw will probably work just fine. You will need to flatten the bottom of the plane so that it will be able to cut crisp clean shaving off. Start with 220 grit and work it over until you have uniform scratches upon the entire body. You actually don’t need to have the entire bed perfectly flat. Only the front of the bed, the front and back of the mouth and the back of the bed need to be co-planer with each other. If you happen to have a hollow area between the back of the mouth and the back of the bed, it’s perfectly fine. Once you have uniform scratch marks with 220 grit paper, switch to 320, then 400 and so forth until you have a nice clean bed with the 600 grit paper.

   

Next and most importantly, you need to sharpen the blade. I own a Tormek sharpener so I use my Tormek to grind a 25 degree bevel on my irons. After I sharpen and flatten the back of the iron with the fine grit of stone I switch over to my 4000 grit water stone and continue to sharpen the burr off. I then finalize the edge with my 8000 water stone. Sharpening to this magnification gives me an edge that stays sharper than simply using my Tormek alone.

  

Now it’s time to see the results of your work. Take a piece a wood and start planing it. You will need to adjust the position of the frog and depth of the blade in order to achieve a clean cut. Since you’re using a jointer plane the tolerances of mouth opening isn’t as critical as it would be for a smoother. You’re not trying to achieve .002″ thick shavings with a jointer. A jointer is a medium cut plane that is used to clean up joints and panels so that other planes can finish the job. A shaving of .005 to .010″ should work just fine.

With about an hours worth of work, you can a have a perfectly usable plane and save hundreds of dollars as opposed to going out and buying a brand new plane off the shelf.

**** Word to the wise: If you’re a beginning woodworker and are considering spending a few hundred bucks on a 6″ motorized jointer, pick up one of these hand jointers for $30.00 and learn to use it. I no longer even use my 6″ motorized jointer anymore.

UPDATE 4/17/17 — Forget about buying a Stanley No 7 for $30.00. Prices have gone way up since I wrote this post in 2011. If you buy one on eBay, you’ll pay $100 or more. If you’re lucky, you may find one at a flea market or antique show for less, but don’t count on it.

Discovering the faults of production type chairs

My wife and I were browsing Half Price Books tonight when a wooden chair caught my eye. What I saw was a screw on the top of the chair where the side was mortised into the top.  So I grabbed my phone and took a couple of pics.

I turned the chair around and I saw the tenon and how small it was in relation to the size of the mortise.

The amount of slop on the tenon was astonishing. Seemed like there was a 3/16″ play all around the tenon. I couldn’t tell how much difference there was between the thickness of the tenon and the width of the mortise but there wasn’t any glue residue on the tenon. You would think with all of the stress put on a chair that the manufacturer would be more attentitive to the proper size of the mortise and tenon joints in their furniture. Just another reason why it’s better to buy furniture from craftsmen who care about their work.